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MonelK-500合金真空感应熔炼工艺优化依据及控制
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北京科技大学 材料科学与工程学院

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北京市自然科学基金面上项目(No.2242042)


Optimization Basis and Control of the Vacuum Induction Melting Process for Monel K-500 Alloy.
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School of Materials Science and Engineering, University of Science and Technology Beijing

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北京市自然科学基金面上项目(No.2242042)

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    摘要:

    Monel K-500合金在真空感应熔炼(VIM)浇注过程中铸锭上部易出现大量缩孔缺陷,导致成材率低、质量差。为解决该问题,本文通过Jmat-Pro热力学计算对Monel K-500合金的热物性能及凝固过程进行了探究。实验结果表明:Monel K-500合金的凝固区间在1250℃-1350℃之间;凝固路径为:L→L+γ→L+γ+MC→γ+MC+M7C3→γ'+γ+MC+M7C3;凝固过程中随着残余液相百分数减小,Ni元素发生负偏析,Cu元素发生正偏析。将热力学计算结果结合有限元(FEM)模型,对工业中6t级Monel K-500合金真空感应熔炼浇注过程进行模拟计算,并将结果和实际真空浇注的感应锭上部缩孔缺陷形状及尺寸进行对比,验证浇注模型的可靠性。此外,本文依托该模型探究了不同浇注参数对真空感应锭缩孔缺陷的影响,结果表明:添加冒口对真空感应锭中缩孔缺陷的改善最大,随着冒容比增大,真空感应锭中缩孔缺陷体积大幅降低,在冒容比为20%时,真空感应锭中无缩孔缺陷;浇注速度在2.5kg/s-17.5kg/s范围时,随着浇注速度降低,真空感应锭中缩孔体积减小,但小于7.5kg/s时缩孔缺陷向真空感应锭内部移动。

    Abstract:

    During the vacuum induction melting (VIM) casting process of Monel K-500 alloy, a large number of shrinkage defects are likely to occur in the upper part of the ingot, resulting in low yield and poor quality. To address this issue, this paper investigates the thermal and physical properties and solidification process of Monel K-500 alloy through thermodynamic calculations using JMat-Pro. The experimental results show that the solidification range of Monel K-500 alloy is between 1250°C and 1350°C; the solidification path is: L→L+γ→L+γ+MC→γ+MC+M7C3→γ'+γ+MC+M7C3; During the solidification process, as the percentage of the residual liquid phase decreases, Ni exhibits negative segregation, while Cu exhibits positive segregation. Combining the thermodynamic calculation results with a finite element (FEM) model, a simulation of the industrial vacuum induction melting casting process for 6 tons of Monel K-500 alloy was conducted. The simulated results were compared with the actual shape and size of the shrinkage defects in the upper part of the induction ingot to verify the reliability of the casting model. In addition, this paper explores the effects of different pouring parameters on shrinkage defects in the vacuum induction ingot based on the model. The results show that the addition of a riser has the most significant improvement on the shrinkage defects in the vacuum induction ingot. As the riser volume ratio increases, the volume of shrinkage defects in the ingot body decreases significantly, with no shrinkage defects present in the ingot body at a riser volume ratio of 20%. When the pouring speed is in the range of 2.5 kg/s-17.5 kg/s, the volume of shrinkage defects in the vacuum induction ingot decreases as the pouring speed decreases; however, below 7.5 kg/s, the shrinkage defects move inward within the ingot body.es; however, below 7.5 kg/s, the shrinkage defects move inward within the ingot body.

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孙攀贺,李澍,江河,董建新. MonelK-500合金真空感应熔炼工艺优化依据及控制[J].稀有金属材料与工程,,().[Sun Panhe, Li Shu, Jiang He, Dong Jianxin. Optimization Basis and Control of the Vacuum Induction Melting Process for Monel K-500 Alloy.[J]. Rare Metal Materials and Engineering,,().]
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  • 收稿日期:2024-11-13
  • 最后修改日期:2025-02-07
  • 录用日期:2025-02-21
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